September 22, 2008 - The drivetrain worked out well. The engine was flexible enough that even when I lost the top 2500 rpm of the rev range, I was still able to make good time. It used almost no oil over 2200 km of driving including 500+ km of full-throttle stages. More power would have been nice, but I think that's the lament of every driver.
I launched the car with smoking tires every single time and there were no problems. I did misjudge the start a couple of times and left the line with lots of clutch slip instead of tire smoke, but the clutch took it without complaint.
The misfire? Well, I'll figure out what it was shortly. I did discover yesterday that one of the wires to the intake air temperature sensor is broken. There was about 8" of unsupported wire leading up to the sensor, and the vibration and pounding made this about 6" too much. I'll fix it when I get a chance and see if that solves the problem. tags: post-race, ergonomics |